Creager
Explorer Addict
- Joined
- October 11, 2004
- Messages
- 2,780
- Reaction score
- 4
- City, State
- Charlotte, NC
- Year, Model & Trim Level
- '92 Sport 4x4
Yep she’s running lean, the question is... why?
The last time I rebuilt the top-end of this motor was a few weeks ago, prior to that was January (yeah three months between rebuilds, Hey I’m pretty good at it now). Ill try and explain the sequence of events.
I removed the heads in Jan to chase down a problem with extensive oil and coolant loss. Head was cracked, guides shot. Stock heads were brought in, valves grinded, deck milled, guides replaced with phosphorous bronze guides of similar dimensions (stock Volvo part I believe?). Afterwards I sealed up the top end and she was running great, haven’t lost a drop of oil or coolant since...
A few weeks later I’m driving' home on a 120 mile trip from Boone, NC when the check engine light comes on. At the time I was alarmed, but I couldn’t do much so I just took it easy on her. Then, at some point as I was cruising up and down the mountains she started miss-firing BAD. I guessed she was running on 4 cylinders, and I was right. Removed the spark plugs, plugs that came out of cylinders 2 & 4 were completely melted, no electrode left (surprizingly, the other 4 looked perfect, nice golden color). Threw in some new plugs and limped her home. Cylinder 2 had lost ~30lbs of compression, and cylinder 4 was at zero. Removed those heads, and found a dime sized hole in the exhaust valve on cylinder 4.
Lost for an explanation I went to my machinist. He helped me out, grinded all the exhaust valves for free, replaced the one blown valve for cost, and even kernelled out some of the exhaust guides (fo free!) as he felt he they needed a little more clearance (as he was the one that put them in there). Either way, he felt that it was obvious I had a fueling problem or an air leak.
So I got it all back together and ran the codes,
KOEO test brings up 172 in the memory codes,
KOER test also brings up 172 and only 172.
First things first, fuel pressure...
I hooked up my fuel pressure gauge, and turned the key without starting...
First turn of the key... 12lbs (not really good...)
Second turn of the key... 38lbs (much better)
Third turn of the key... 40lbs (just what I like to see)
Then, I checked the pressure with the engine running
At idle the pressure sits between 32-35lbs.
At WOT, the pressure drops to 28lbs, the lowest I saw it go.
These numbers indicate to me, that I have solid fuel pressure.
But just to make sure, the two cylinders that madly leaned out, got brand new fuel injectors.
On to checking the vacuum...
The lower and upper intakes were just recently sealed with new gaskets and torqued to spec (using the Haynes manual, the instructions Fel-Pro includes with their gaskets, and snip-it’s from the Ford Manuals.) So I know there is no leak here.
So moving forward, I found a can of starting fluid in my hand, and sprayed a mess on every vacuum line I could find... FPR, PCV system, A/C lines, Break booster, cruise control, everything I could think of.
Although the RPM never changed, nor did I see any smoke from the exhaust.
So on to the various sensors and circuits.
TPS is set to ~.965v
MAF cleaned, and swapped with the Factory unit (had a PRO-M on there).
On to the 02 sensor...
First I ran a ground from the computer to the block, to make sure.
The best I could come up with was by using a voltmeter to measure the voltage coming off the 02 sensor. Ford used 4 wires to mate up the engine harness with the sensor. An orange wire, a orange with black stripe, a grey with blue stripe, and a black with a white stripe. One of the orange wires stayed constant 12v, the other orange wire and grey wire would be at .45v with the engine off, while the black one would usually be around nothing.
With the engine running the black wire seemed like the right one (I don’t really know) but it was constantly switching around .45v. The voltage was pretty much all over the place, from .01v-.4v then it would jump .6v-.9v;
There were a few times, after the CEL would illuminate, that the readings would get 'stuck' in a certain range... At one point the readings stayed between .01v-.1v while the engine RPM hovered around 2000. Then another time, the reading didn’t move from .80-.83 while at 2000 RPM. (I figured that would throw a rich code, but it still said 172) My research indicates that a bad 02 sensor could get stuck like this, but it seems like I’m really running lean! I pulled the plug out of cylinder number 4 and it was clean... TOO clean. Whitish, lean... lean meat no good for my beefy engine!
my theory...
From what I understand, when the CEL becomes illuminated the ECM automatically attempts to judge fuel/air mixture by pre-calculated ratios from the factory (?). Now, since I’m running a much different cam, and have serious vacuum getting sucked into this thing, what the computer thought was a safe default setting, may be leaner then normal, especially at RPMs higher then 3000. Which could explain the massive lean out, but the 02 sensor is actually sending the computer a lean code which illuminated the CEL in the first place...
I’m confusing myself!
The last time I rebuilt the top-end of this motor was a few weeks ago, prior to that was January (yeah three months between rebuilds, Hey I’m pretty good at it now). Ill try and explain the sequence of events.
I removed the heads in Jan to chase down a problem with extensive oil and coolant loss. Head was cracked, guides shot. Stock heads were brought in, valves grinded, deck milled, guides replaced with phosphorous bronze guides of similar dimensions (stock Volvo part I believe?). Afterwards I sealed up the top end and she was running great, haven’t lost a drop of oil or coolant since...
A few weeks later I’m driving' home on a 120 mile trip from Boone, NC when the check engine light comes on. At the time I was alarmed, but I couldn’t do much so I just took it easy on her. Then, at some point as I was cruising up and down the mountains she started miss-firing BAD. I guessed she was running on 4 cylinders, and I was right. Removed the spark plugs, plugs that came out of cylinders 2 & 4 were completely melted, no electrode left (surprizingly, the other 4 looked perfect, nice golden color). Threw in some new plugs and limped her home. Cylinder 2 had lost ~30lbs of compression, and cylinder 4 was at zero. Removed those heads, and found a dime sized hole in the exhaust valve on cylinder 4.
Lost for an explanation I went to my machinist. He helped me out, grinded all the exhaust valves for free, replaced the one blown valve for cost, and even kernelled out some of the exhaust guides (fo free!) as he felt he they needed a little more clearance (as he was the one that put them in there). Either way, he felt that it was obvious I had a fueling problem or an air leak.
So I got it all back together and ran the codes,
KOEO test brings up 172 in the memory codes,
KOER test also brings up 172 and only 172.
First things first, fuel pressure...
I hooked up my fuel pressure gauge, and turned the key without starting...
First turn of the key... 12lbs (not really good...)
Second turn of the key... 38lbs (much better)
Third turn of the key... 40lbs (just what I like to see)
Then, I checked the pressure with the engine running
At idle the pressure sits between 32-35lbs.
At WOT, the pressure drops to 28lbs, the lowest I saw it go.
These numbers indicate to me, that I have solid fuel pressure.
But just to make sure, the two cylinders that madly leaned out, got brand new fuel injectors.
On to checking the vacuum...
The lower and upper intakes were just recently sealed with new gaskets and torqued to spec (using the Haynes manual, the instructions Fel-Pro includes with their gaskets, and snip-it’s from the Ford Manuals.) So I know there is no leak here.
So moving forward, I found a can of starting fluid in my hand, and sprayed a mess on every vacuum line I could find... FPR, PCV system, A/C lines, Break booster, cruise control, everything I could think of.
Although the RPM never changed, nor did I see any smoke from the exhaust.
So on to the various sensors and circuits.
TPS is set to ~.965v
MAF cleaned, and swapped with the Factory unit (had a PRO-M on there).
On to the 02 sensor...
First I ran a ground from the computer to the block, to make sure.
The best I could come up with was by using a voltmeter to measure the voltage coming off the 02 sensor. Ford used 4 wires to mate up the engine harness with the sensor. An orange wire, a orange with black stripe, a grey with blue stripe, and a black with a white stripe. One of the orange wires stayed constant 12v, the other orange wire and grey wire would be at .45v with the engine off, while the black one would usually be around nothing.
With the engine running the black wire seemed like the right one (I don’t really know) but it was constantly switching around .45v. The voltage was pretty much all over the place, from .01v-.4v then it would jump .6v-.9v;
There were a few times, after the CEL would illuminate, that the readings would get 'stuck' in a certain range... At one point the readings stayed between .01v-.1v while the engine RPM hovered around 2000. Then another time, the reading didn’t move from .80-.83 while at 2000 RPM. (I figured that would throw a rich code, but it still said 172) My research indicates that a bad 02 sensor could get stuck like this, but it seems like I’m really running lean! I pulled the plug out of cylinder number 4 and it was clean... TOO clean. Whitish, lean... lean meat no good for my beefy engine!
my theory...
From what I understand, when the CEL becomes illuminated the ECM automatically attempts to judge fuel/air mixture by pre-calculated ratios from the factory (?). Now, since I’m running a much different cam, and have serious vacuum getting sucked into this thing, what the computer thought was a safe default setting, may be leaner then normal, especially at RPMs higher then 3000. Which could explain the massive lean out, but the 02 sensor is actually sending the computer a lean code which illuminated the CEL in the first place...
I’m confusing myself!