jstelmack
Member
- Joined
- December 2, 2011
- Messages
- 21
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- Year, Model & Trim Level
- 1994 Mazda B2300, 5sp, ba
From previous thread: 1994 2.3L 5 speed base model Mazda B2300. Engine ran ROUGH, no power, backfired, bogged down etc.
Replaced Fuel pump assy, cleaned tank, new fuel filter. Cleared codes. Added SeaFoam cleaner to tank of fresh gas.
codes 111,111 and that's all. Looks like only "pass" codes under KOEO or KOER tests.
Driving around I can tell it is getting progressively better/more power/no back fires/less bogging down. Suspect the SeaFoam is slowly cleaning out the injectors.
THE PROBLEM - I noticed that, by error, I left the jumper installed on the diagnostic connector. Engine running when I remove the jumper. The engine immediately dropped in RPM and started running noticeably rougher. I did a few drive tests, with jumper installed and jumper removed. When jumper installed the engine performs much better, although still lacking typical power. With jumper removed, the engine bogs down under throttle and has less power. But it does not backfire anymore.
Any ideas what could cause this? Several KOEO and KOER tests have been performed since replacing the fuel pump and clearing codes. Consistently get 111, 111 PASS PASS.
Thanks!
Replaced Fuel pump assy, cleaned tank, new fuel filter. Cleared codes. Added SeaFoam cleaner to tank of fresh gas.
codes 111,111 and that's all. Looks like only "pass" codes under KOEO or KOER tests.
Driving around I can tell it is getting progressively better/more power/no back fires/less bogging down. Suspect the SeaFoam is slowly cleaning out the injectors.
THE PROBLEM - I noticed that, by error, I left the jumper installed on the diagnostic connector. Engine running when I remove the jumper. The engine immediately dropped in RPM and started running noticeably rougher. I did a few drive tests, with jumper installed and jumper removed. When jumper installed the engine performs much better, although still lacking typical power. With jumper removed, the engine bogs down under throttle and has less power. But it does not backfire anymore.
Any ideas what could cause this? Several KOEO and KOER tests have been performed since replacing the fuel pump and clearing codes. Consistently get 111, 111 PASS PASS.
Thanks!