How to: - 1st Gen Gas Tank Fuel Pump Access Panel | Page 6 | Ford Explorer Forums - Serious Explorations

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How to: 1st Gen Gas Tank Fuel Pump Access Panel

Prefix for threads which are instructional.
Sigh of relief - thanks to all who posted - this is awesome info

I dropped a tank on my first 94 EB about 10 yrs ago in 98 degree summer heat and it was NO FUN after getting the pump out i saw the cause of the problem was the two wires inside the tank (power?- red and ground?- black) had actually rubbed themselves together so bad they arced and were welded together !!!YIKES!!!!!! i couldnt believe it didnt go kablammo! should have taken a pic but anyways today my pump went out on my second 94 EB and i was totally bummed about having to drop the tank (which was full of course lol) in the muggy heat here in florida (fireants are crazy here too ouch!!) so i happened upon this great thread and now im really relieved....thanks for everyone's pics, descriptions, and shared expereinces . you all made my day!!

Matt
:exp: :thumbsup:
 



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At 11AM today, I had a no start condition at a convenience store. Thanks to these forums, I accomplished the following:

12PM Vehicle towed home, verified bad pump.

12:45 Back seats removed, access door cut, staring at top of tank, verified 12 volts going in, no gas coming out, no noise of any kind.

2:00 New pump swapped in, key turn, engine starts immediately.

3:00 Everything reassembled, driving down the highway with the AC on and a nice cold glass of ice water.

Basically a 4 hour fix including the tow home. Total cost $200 including tow.

I'm offering these words because, you know, once I saw some pictures and knew other people had no trouble, I jumped right in.

The gas line connections were a pain. The Lisle kit with the white plastic tools didn't work very well. I'd buy something else. Owing to the sharp edges in the trap door that I cut, this was a 3 band-aid job.
 






At 11AM today, I had a no start condition at a convenience store. Thanks to these forums, I accomplished the following:

12PM Vehicle towed home, verified bad pump.

12:45 Back seats removed, access door cut, staring at top of tank, verified 12 volts going in, no gas coming out, no noise of any kind.

2:00 New pump swapped in, key turn, engine starts immediately.

3:00 Everything reassembled, driving down the highway with the AC on and a nice cold glass of ice water.

Basically a 4 hour fix including the tow home. Total cost $200 including tow.

I'm offering these words because, you know, once I saw some pictures and knew other people had no trouble, I jumped right in.

The gas line connections were a pain. The Lisle kit with the white plastic tools didn't work very well. I'd buy something else. Owing to the sharp edges in the trap door that I cut, this was a 3 band-aid job.

For the tool to remove the plastic lines, i bought a universal tool from advance autoparts that Says its for ford vehicles, and its Metal so it can be used over and over. It fits both Large and small lines. Just my thoughts
 






My turn now. The ex died with no more pump sounds and I checked everything out to verify: fuel pump needs replaced.

Sooo, i'm going to both drop the tank so I can inspect everything under there, and cut the access hole for the future.

Awesome thread! Thanks to everyone including the original poster.
 






Thanks and leaving the seat in

First of all THANK YOU BURNS for the great pics. I left my seat in, held the fold down plate back with a coat hanger. Took a 3/8" titanium drill bit and put it in my drill, found a 1/2"drive deep well socket that was long enough to only leave a 1/4" of the drill tip showing. Drilled holes about a 1/4 inch apart.... I didn't take the "L" shaped jog... just went straight up. Then used a vertical sheet metal nibbler to connect the holes. I made my cover out of aluminum so it wouldn't rust, and simply set it into a large bead of rtv. I also filled my quick connects with dielectric grease to hopefully avoid the rust build up that was such a PITA this time. For anyone doing this in their spare time, I would strongly advise converting to some fuel injection hose and clamps. These quick connects are a nightmare if you live up north where things get so rusty. Thanks again.
 






97 2dr sport

Thanks for this great idea! I'm contributing pics of my 2-door 97 explorer. The fuel pump is directly under the rear driver's side seat.

Here's the view from the passenger door:
pump1.jpg


Here's a closer view from inside:
pump2.jpg



And here's a close-up shot of the hole I cut with the new pump in:
pump3.jpg



The connector on the left is directly in line with the studs that hold the chair in, so you can use them to gauge where to begin. The bottom cut goes right below the stud that holds the plastic guard in, and about an inch past it to the right (pic of that later). There's a thick support connecting the floor to the rest of the chassis next to this stud that didn't look safe to cut through.

I tried to get a picture of it here:
pump4.jpg



Here's a picture of the metal folded down:
pump5.jpg


I used a 3/4" cold chisel that I picked up from Home Depot for under 10 bucks. It took me a little over two hours to get through all the metal, but most of that time was spent trying to figure out how to use a chisel. I'm sure that if you have even basic experience with a chisel then you could do it in under a half hour. Also, BE CAREFUL!!! If you have two inches between the floor and the fuel lines, then you are blessed. If you hit one of these you won't create a spark to start a fire, but you WILL hate yourself when you have to replace the fuel line.
The fuel line tool is whatever generic quick-disconnect tool that Autozone sells. I don't remember what sizes the two fittings are, but I know the box said it was good for all Fords. It doesn't feel like it fits the bigger line, but I managed to get it off with some patience.

pump6.jpg


Here's the plastic thing that goes under the seats. I don't know what it's for, but it doesn't seem too important. Even though I cut around the stud that holds it down, I can still get it back on. I'll probably re-attach it just in case...

All in all this wasn't too bad of a job. It beats the hell out of laying on my back. Unclipping the connector on the frame wall wasn't too bad - I used a flathead jeweler's screwdriver to put a gap in the clip and push the two connectors apart. Clipping the new one in was a bit of a hassle though. I went in from the top and had to twist my arm in a strange, uncomfortable way to get the connectors to line up.
Be sure to air out the vehicle after installing the new pump, and keep the windows open at all times. My tank was about 3/4 full when I did this. I swapped my pump as quick as I could, opened all the doors and windows, and went across the street for a smoke break. When I came back about 10 minutes later, the whole interior still reeked of fuel vapor. I waited probably another 15 minutes before re-entering to clean everything up.
 






What's the consensus on what the best, *common*/inexpensive tool is to cut this out? 4" angle grinder? (unless, of course, you have a fuel leak).
 






That is what we used when doing this. It has never failed us but we did always let it get low on gas just in case.

Just take your time and do not make deep cuts. Take the time to do this one right. Otherwise you may have a fire on your hands.
 






I cut the hole in my 1993 XLT 4x4 using an air chisel. The tin went very easily but when I got to the double thick part it was harder. I drilled starter holes in three corners (front driver side front other and rear other). I hit the double thick part about 6 inches back from the front radius (down). It was too hard for the chisel so I drilled 1/4" holes every 1" or so in an arc from the spot where the double thick started to the irear hole drilled earlier. Then I cut the upper sheet first with the chisel, followed by the heavier gauge material below it afterward using the holes as starting points. The tank was farther back than others showed. I haven't done so yet, but it looks like the unit can come out without too much maneuvering. The problem I am having is that the gauge is indicating wrong, I think the float is full.

Note: I used the v-chisel for the sheet metal but it wouldn't do the heavier stuff so I used the regular air chisel blade. It pounded quite awhile but did the job. I can't quite imagine using a hand chisel to do all of that, but I'm old and kinda puny.

Update: I was successful at removing the ring on the pump using lots of WD40 and some patience. The ring got damaged because I used a screw driver on the tabs that stick up. (I just straightened them with a pliers and installed the ring 90 degrees off.) After I got it loose, I pulled the cable connector loose from underneath behind the tank, connected a wire to it and drew it out while pulling the wire in. Then I disconnected the fuel lines (really easy with a metal tool) and the pump came out with some jockeying around. I covered the hole with a towel after cleaning up. I saw that the float was cracked and full. To fix it, I tried cleaning it with a wire brush and soldered the crack all around the depression where the float's rod is inserted. They used a c-shape to encircle the float which fits into a boss all the way around the float. After soldering, I reinserted the float rod and put it back together, using the wire to pull the connector back where I could reach it. Tried it, same problem as before. So pulled it apart again, removed the solder and coated the boss and cracked areas with J B Weld. After drying over night, I reinstalled it. Oops! Now it shows full. Then I realized that I had put the float on backwards according to the picture, the float should not contact the body of the pump. Pulled apart again, reinserted so the float is free. It works showing me 1/4 tank which is about right. Couple of days later it still works so I think the repair was successful and I made a cover plate, reassembled the seats and carpet - looks as good as new. I made the cover plate using some material from an old water heater tank shell. I cut it about 9.5 x 7 and bent both the front over the front lip and the back at about 2.5" in. This fit nicely - I put self-tapping 5/16 drive screws that they used to make my shop; three on the front bend, two at the rear bend and two on the top. Looks pretty good.

BTW, though there is no reason to be stupid about it, but gasoline is very difficult to get started burning - you are better off with a full tank of fluid rather than less than that with a partial tank of vapors. As long as there is not enough heat or pressure from the flash to disturb the gasoline or start the gasoline burning, the worst you will get is a scare as the vapor mixture ignites and burns - the chances are that this will not cause anything to happen to the liquid gasoline - however, better to err on the side of caution and avoid the experience entirely (it's one you can live without). It won't blow up in a fireball like in the movies without some assistance.
 






I used a 4" angle grinder, It did the job but i was worried about fires... at the time if i had better tools i woulda used em
 






At 11AM today, I had a no start condition at a convenience store. Thanks to these forums, I accomplished the following:

12PM Vehicle towed home, verified bad pump.

12:45 Back seats removed, access door cut, staring at top of tank, verified 12 volts going in, no gas coming out, no noise of any kind.

2:00 New pump swapped in, key turn, engine starts immediately.

3:00 Everything reassembled, driving down the highway with the AC on and a nice cold glass of ice water.

Basically a 4 hour fix including the tow home. Total cost $200 including tow.

I'm offering these words because, you know, once I saw some pictures and knew other people had no trouble, I jumped right in.

The gas line connections were a pain. The Lisle kit with the white plastic tools didn't work very well. I'd buy something else. Owing to the sharp edges in the trap door that I cut, this was a 3 band-aid job.

Where did you get a pump for $200 or less???

I cannot find one for mine for under $350. Although I am looking for the whole assembly. Float sending unit and all. Also I was stupid enough to drop the tank, instead of going on here to see if it was possible to cut a hole, I might just cut one so that if it ever happens again I don't have to drop the tank.
 






This is a great idea and is easy to do. All you need is a socket set to remove the seat (4 bolts); a hammer and a cold chisel to make the hole. If you have the desire to get an air chisel, it would make the job go much faster, but I did this by hand in about 20 minutes.

'96 Explorer 4WD - 4.0L 6cyl.
ExplHole.jpg


Now - what are the chances I can get those rusty bolts to come out?
 






This thread is awesome! Great work everyone.
 






can this be used for a 98 XLT?

Does the thicker cross member have to be cut slightly?
 






great pics

After replacing the window motor "hockey pucks" and finding out that the bozos left a dimple that I had to drill to find the missing bolt, I no longer fear the cut and paste method of auto repair. BTW my son's 1998 Honda Civic has a neat cutout in place over the pump. Same idea, remove back seat, remove cutout, remove and replace pump, reassemble. I did it with cordless tool kit in about an hour. I'm doing fuel filter first - if results aren't as desired - pump cut is next! Thanks again!
 






More pics!

As clean as I could get it with a sazall.. ;)
CIMG0094.jpg

A side shot
CIMG0095.jpg

Preparing
CIMG0099.jpg


CIMG0098.jpg


CIMG0100.jpg
 






New pump installed!
CIMG0101.jpg

Getting ready to apply the stitches
CIMG0103.jpg

Silicon and weatherstripping.
CIMG0113.jpg

Used a piece of sheet metal I picked up from home depot
CIMG0102.jpg

These things work great!!!
CIMG0127.jpg

The final look before I put the carpet back down and install the seat!
CIMG0126.jpg
 












They make metal & plastic access panels for houses in many different sizes & shapes. Here are some examples:
http://www.proproductssales.com/products_retail/index.php?cPath=6
CircularAccessPanel.jpg
Novopanel-Softline-Access-Panel-Access-Door.jpg


The panel on the right looks like a fire rated access panel :thumbsup: It may fit with some slight modifications and would be a nice way to trim things off.

This thread is excellent! I've learned a lot from it. I kinda wonder why it is in the waxing washing, wheel cleaning and body work section :scratch: :D
 



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