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Can your engine do this?!...

DeepBlueSC

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Older story, but thought it may 'help' those thinking about an EcoBoost engine...

A production EcoBoost V-6 engine, serial number 448AA, was randomly selected off the assembly line at Ford’s Cleveland engine plant. The dual-overhead-cam power plant was shipped to dynamometer cell 36B in the Ford Dearborn engine labs and run for 300 hours to replicate the equivalent of 150,000 customer miles, including repeated temperature-shock runs when the engine was cooled to minus 20 degrees Fahrenheit and then heated to 235 degrees.

The engine was then shipped to Ford's Kansas City truck plant and installed in an F-150 4X4 crew-cab pickup. It was driven to Nygaard Timber in Astoria, Ore., and put to work as a log skidder, dragging a total of 110,000 pounds of logs across the ground to demonstrate its 420 pounds-feet of torque.

From there, the truck was driven across the country to Homestead Miami Speedway, where it was hooked up to a trailer carrying two of Richard Petty’s Ford Fusion race cars, a load of 11,300 pounds, and run continuously around the track for 24 hours, averaging 82 mph and covering 1,607 miles.

It was then taken to Davis Dam in Arizona, where it bested both the 5.3-liter Chevy Silverado V-8 and the Ram 5.7-liter Hemi V-8 in an uphill towing contest pulling 9,000 pounds up a 6 percent grade on Highway 68.

Finally, the 3.5-liter twin-turbo EcoBoost engine was shipped to Mike McCarthy’s race shop in Wickenburg, Ariz., and installed in his 7,100-pound F-150 race truck. McCarthy practiced locally for 1,200 miles and raced the truck in the SCORE Baja 1000, the toughest off-road race in North America, finishing first overall in the new Stock Engine class after 1,062 race miles.

McCarthy said the engine’s fuel economy was so good compared with his previous V-8 engines that he was able to skip two planned fuel stops during the Baja event, which helped him win the class.

After Baja, the thoroughly thrashed and raced engine was shipped back to Ford headquarters in Dearborn, Mich., and dyno-tested once again. It was found to produce 364 horsepower and 420 pounds-feet of torque, just one horsepower less than its rating and exactly the same output as its nominal torque rating, according to Ford.

A leakdown test was performed to measure how well the engine’s 24 intake and exhaust valves and piston rings were still able to seal the cylinders. One cylinder was found to have a cautionary 13 percent air loss past the combustion chamber’s seals, while all other cylinders were acceptable with single digits of air leakage.

Oil pressure at idle on the dyno was normal, in the mid-40 psi range.

After the dyno, engine 448AA, which had never been opened or inspected, was shipped to the Detroit auto show where it was torn down for inspection in front of a live audience of more than a thousand Ford engine enthusiasts and their families.

The teardown was narrated for the audience by Jim Mazuchowski, Ford’s chief engineer for V-6 engines. Powertrain engineer Phil Fabien explained the advantages of things like turbocharging, direct fuel injection and twin independent variable cam timing while engine technicians Chris Brown on the right bank and Chris Rahill on the left bank took the engine apart using a pair of air wrenches and hand tools.

As they went, the engine parts were laid out on three huge tables so that when the tear-down was complete, the engineers and the audience could take a closer look. During the tear-down, engineers Steve Matera, Kirk Sheffer and Jeanne Wei organized the parts and made some key measurements.

Valve lash, which measures valvetrain clearance between the camshafts and valves, was checked at 0.17 mm on the intakes and 0.38 mm on the exhausts. That’s well within normal range for both, according to Ford. Crankshaft end play was measured at 0.12 mm, also acceptable.

The timing chain, which controls valve timing and synchronizes engine operation, was still within normal tolerances. With age, a timing belt loses tension, and a hydraulically operated timing chain tensioner is used to compensate for slack. The tensioner has 10 teeth that work like a ratchet to maintain tension. The EcoBoost V-6 used three teeth, well within the timing chain’s operating specs.

The valves had carbon deposits similar to that found on piston combustion surfaces.

Visual inspection of the cylinder heads, twin turbos, piston crowns, ring lands, rod bearings and cylinder bores by the engineers showed no major signs of anomalous wear after 163,000 miles of endurance testing. The main bearings showed cosmetic grooves but not excessive wear through the metal.

Engineer Wei said each and every part would be taken back to Ford’s labs to be checked with scales, cameras, lasers, micrometers and other measuring tools to get the final details on the rich, full life of EcoBoost V-6 engine 448AA.
 



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Are you talking about when the 3.5L was initially marketed? I remembered those advertisements. There was a vacuum leak on one of the cylinders after all these tests though. Other than that, the Ecoboost did really well.
 






I need to figure out a way to put one in a first gen!
 






This was from 2011 when the motor was first introduced.

FYI, it didn't have a vacuum leak, it showed a 13% drop in a leakdown test. Basically, nitrogen is introduced into the cylinder and then the amount of N2 that gets past the valve seats and piston rings is indicated in % of N2.

Essentially, while not perfect it's not terrible either. All other cylinders showed a single digit drop in this test. So let's say for the sake of argument the others were at 9%. That's only a 4% difference. Considering the absolute abuse this motor was put through, I would argue that it's an acceptable trade off. Also keep in mind they used regular motor oil, no synthetics or synth blends.
 






N3 not N2 Pay attention!
 






i remember watching the video on this, it was pretty cool.
 






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