patmac6075
Member
- Joined
- September 8, 2015
- Messages
- 28
- Reaction score
- 0
- City, State
- MKE
- Year, Model & Trim Level
- '98 Explorer
Just finished changing out my fuel filter on the '98 4.0 OHV. What a PITA!
First off I bought a set of those plastic quick disconnects.....total waste of money! I could not get enough leverage on the plastic "ears" to get them under the locking device, they just bent and then finally broke. I ended up getting the KD Tools metal tool($5.00+)....it's the one that's shaped like an X. Those worked much better.
Although my car had spent much of its life in New Mexico and is very clean underneath, the connectors were very corroded and did not want to release. I sprayed them with SeaFoam's Deep Creep for three days and was finally able to get them to release. I installed the new filter and now I couldn't get those fittings to "click" back on....back to the Deep Creep, I sprayed those fittings to lubricate them and worked the locking mechanism with my KD tool and finally I was able to get the fittings to snap back into place! Initially, I thought this was going to be a 20 minute job....took me 3 days.
Long story short, was well worth the effort, as the engine is running much smoother now.
First off I bought a set of those plastic quick disconnects.....total waste of money! I could not get enough leverage on the plastic "ears" to get them under the locking device, they just bent and then finally broke. I ended up getting the KD Tools metal tool($5.00+)....it's the one that's shaped like an X. Those worked much better.
Although my car had spent much of its life in New Mexico and is very clean underneath, the connectors were very corroded and did not want to release. I sprayed them with SeaFoam's Deep Creep for three days and was finally able to get them to release. I installed the new filter and now I couldn't get those fittings to "click" back on....back to the Deep Creep, I sprayed those fittings to lubricate them and worked the locking mechanism with my KD tool and finally I was able to get the fittings to snap back into place! Initially, I thought this was going to be a 20 minute job....took me 3 days.
Long story short, was well worth the effort, as the engine is running much smoother now.