OK, this is what all I did today (summarized). Changed the filter and took out all six solenoids, cleaned them good with the brake cleaner, checked the Ohms on all 6 (they read fine) and refilled with 4qts of new fluid. Now that I type it out it seems like we didn't do much of anything :fire:

. We didn't really see a way to spray the EPC solenoid from inside the screen so we just sprayed the hell out of the screen from the outside as good as possible.
It still does the 2-3 shift deal though maybe not quite as bad (might just be psychologically better if you know what I mean). It still doesn't have the pep I think it shouldin first (like I am half way on the clutch in a 5spd). Though if I drop it into Manual 1 it seems to do much better. The O/D OFF light is still very intermittent and I can't really decipher if the tranny does worse (or better) with the O/D OFF light blinking. It has kind of had this oil-like burning smell though since I have had it (should have been a first sign there not to buy it, I know). Frustrating as can be!!! I might be forced to just take it somewhere and trust me, that is the last thing I want to do b/c I never take my vehicles anywhere except to get tires.
There are a few things I have questions/concerns about during the "process" today:
** When I was pulling out the shift solenoid, next to the EPC solenoid, something that looked like a piece of a VERY small gasket came with it. I took a picture but it might be a few days till I can get it posted. I didn't see anything that resembled where it might have come from.
**When my dad and I were pouring out the old fluid from the container it dripped into, we found 3 VERY small metal "things". Not sure how to explain them other than they were the size of the tip of a pen or so. Not really ball shaped but maybe more of a cylinder shape....again, VERY small.
**The shift solenoid on the side with only two, closest to the front of the truck.....when I was putting it back in it was the only one that had a spring pushing it back out. To the point where I had to hold it in while I put the retaining bracket back on. Was it supposed to be pushing out like that? None of the others did.
Finally, I am going to Louisiana (850ish miles round trip) this coming weekend and the truck seems fine in 4th and 5th I think (2,000rpm at 60mph).....do you think it will make it for this one trip and I will get it in the shop or something when I get back?
A lot of info but I would be Greatly appreciated for Brain or Chris (or anyone else)to give me some feedback or what you can tell me, if anything.
Thanks a lot!!
Geoff