OK, she's back together. running well enough, still not perfectly. But I have a few questions reguarding why I even had to do this.
first off, I had NO smoke emitting from my exhaust, so there was NO oil inside the combustion aspect of the motor.. When I got to both gaskets.. the gaskets looked fine. (I even steam cleaned the motor prior to the replacement and saw no oil leak after about 50 *lightly* driven miles).
I replaced the fuel Injectors, and I'm wondering if that was my real culprit. (Number 3 and 6 low compression - rough Idle) I hate to monday morning quarterback - but its just been bothering me why I had SOME signs (HC's in the radiator - detected by that same shop - who "passed" the smog check it had 4 days before).
The engine was running fine until compression dropped in the number 3 and number 6 cyl SIMUTANEOUSLY (I dont see how both gaskets could've gone at once.. but its possible I presume). I also had a diagnostic done - it was only a number 3 cyl. misfire. with a bank 2 lean code with it.
Was the shop I took it to just trying to gouge me for un-needed work? Thinking that I was not mechanically inclined enough to figure it out on my own?
Any input here would be appreciated.