Mettler
Well-Known Member
- Joined
- February 19, 2009
- Messages
- 226
- Reaction score
- 1
- City, State
- Monroe, WA
- Year, Model & Trim Level
- 98 exploder sport 4x4
So awhile back I posted a thread titled, is my A4LD terminal? The answer to that question is YES. It finally pooped out on me yesterday. Im not really stressed about it cause I knew it was coming from the day I bought it. I was lucky enough to get 22k miles out of it. This is what happened.
Awhile back I was hearing a metal rubbing sound like a bolt working its way out somewhere, but only while I was at a stop, in gear. After bout 3 months that went away.
As the season changed and the weather got colder, it started not wanting to shift into 2nd first thing in the morning. But after it did once, it would work fine for the rest of the day. It also felt at times like the motor was working harder to push the rig down the road than other times. Then sometimes it felt like I didnt need to use as much throttle to get to speed.
Well yesterday it was running good. I felt what seemed like a delayed engagement into first when leaving from a stop. It had been doing that occasionally but worsening.
I came to a stop at a light just before I got on the freeway. When the light turned green and I began to accelerate it felt like I just bumped it into neutral. Except that it still had some pressure. If i revved up to like 4k to 5k it would just barely move. Was just enough to get me off the road. It also didnt leak out a bunch of ATF. Infact I only observed a spot no bigger than a dollar bill.
So now, being an apt dweller and unemployed, I have to rip it out and rebuild. I have all the time in the world and nowhere to work. More punches to roll with. I'll figure it out. Any hoo, so thats what happened.
Any guesses as to what might have happened internally? Im gonna buy a new governor, and a master rebuild kit. It'll be nice to have a new tranny.
Awhile back I was hearing a metal rubbing sound like a bolt working its way out somewhere, but only while I was at a stop, in gear. After bout 3 months that went away.
As the season changed and the weather got colder, it started not wanting to shift into 2nd first thing in the morning. But after it did once, it would work fine for the rest of the day. It also felt at times like the motor was working harder to push the rig down the road than other times. Then sometimes it felt like I didnt need to use as much throttle to get to speed.
Well yesterday it was running good. I felt what seemed like a delayed engagement into first when leaving from a stop. It had been doing that occasionally but worsening.
I came to a stop at a light just before I got on the freeway. When the light turned green and I began to accelerate it felt like I just bumped it into neutral. Except that it still had some pressure. If i revved up to like 4k to 5k it would just barely move. Was just enough to get me off the road. It also didnt leak out a bunch of ATF. Infact I only observed a spot no bigger than a dollar bill.
So now, being an apt dweller and unemployed, I have to rip it out and rebuild. I have all the time in the world and nowhere to work. More punches to roll with. I'll figure it out. Any hoo, so thats what happened.
Any guesses as to what might have happened internally? Im gonna buy a new governor, and a master rebuild kit. It'll be nice to have a new tranny.