MuscleJunkie
Elite Explorer
- Joined
- April 14, 2007
- Messages
- 1,028
- Reaction score
- 352
- Year, Model & Trim Level
- '00 Ford Explorer LTD AWD
I've attached three dyno sheets from my experience (so far) with the Powerdyne BD-11a Supercharger and the Powerdyne XB-1A supercharger.
Obviously, the dyno results from the XB-1A are just preliminary dyno tuning numbers and I honestly feel there is a considerable amount to pull out of this setup. Hoping the community here can take a look at these past results and give some input
These are the next dyno runs with the new Powerdyne XB-1a and 16 fin MID billet impeller (Si Trim)
So initially I mentioned that we thought there was a boost leak in the WTA intercooler. The WTA intercooler system was leak checked (up to 20 PSI - maybe 5 to 10 minutes?) and no leaks were found. It was determined that the cap on the intercooler system reservoir cap was letting expanding intercooler coolant escape through the pressure hole. Remember, the intercooler cooling system is a closed system. No leaks were found in that system. Installer thinks the system was filled too high and is going to come up with a revised system for the reservoir. A smoke test was also performed and nothing was noted. We are still investigating what other issues there possible could be.
Obviously, I think we all expected to see a bigger/better result from the XB-1a. At the moment, they do not feel there is a boost leak. They think "maybe" this could be related to belt-slip with the 2.7 pulley and we are further investigating this. Belt tension is going to be checked and additional pulls with the 2.7 and 2.8 pulleys will be made with a full boost level recording (since the dyno boost gauge during the tuning pulls wasn't functioning consistently ) and see where we are at that point.
Obviously, the dyno results from the XB-1A are just preliminary dyno tuning numbers and I honestly feel there is a considerable amount to pull out of this setup. Hoping the community here can take a look at these past results and give some input
- RWHP 303.07 - Torque 336.51
-
- This was the last dyno of the BD-11A before the rebuild by Jon Bond Performance and original bearing failure.
- I was running the following pulley combo for this pull
-
- 2.7 (2.65) SC Pulley and 6.5 (6.485) crank pulley
- Stock Impeller, stock belt and stock bearings
- Pull cutoff RPM was ~ 5000 rpm
-
- Max blower rpm 36,712 - 37,319
- Boost level observed with this pull was right at 6lbs
- RWHP 287.50 - Torque 337.08
-
- This was the 1st dyno after the rebuild of the BD-11a by Jon Bond Performance
- The following work was done by Jon Bond
-
- New bearings
- Billet Impeller
- New internal belt
- I was running the following pulley combo for this pull
-
- 2.8 (2.86) SC Pulley and 6.5 (6.485) crank pulley
- Pull cutoff RPM was ~ 4800 rpm
-
- Max blower RPM 33,195 - 33,985
- Boost level observed during this pull was in the high 5lb range.
These are the next dyno runs with the new Powerdyne XB-1a and 16 fin MID billet impeller (Si Trim)
- RWHP 268.06 - Torque 304.89
-
- Pull cutoff RPM was 4800 rpm
- I was running the following pulley combo for this pull
- 3.1 SC Pulley and 6.5 (6.485) crank pulley
-
- Max blower RPM 34642 - 34722
- The approximate boost level observed during this pull was in the 4lb range
- The next 3 runs were with the below SC and crank pulley combos
-
- RWHP 295.31 - Torque 325.30
-
- Pull cutoff RPM was ~ 5600 rpm
- RWHP 296.17 - Torque 326.34
-
- Pull cutoff RPM was ~ 5600 rpm
- RWHP 297.52 - Torque 329.53
-
- Pull cutoff RPM was ~ 5600 rpm
- The pulley combo I was running for these (3) pulls was
- 2.7 (2.65) SC Pulley and 6.5 (6.485) crank pulley
- Max blower RPM 46511 - 47279
- The approximate boost level observed during the last 3 pulls was in the 6psi to just at 7psi range
So initially I mentioned that we thought there was a boost leak in the WTA intercooler. The WTA intercooler system was leak checked (up to 20 PSI - maybe 5 to 10 minutes?) and no leaks were found. It was determined that the cap on the intercooler system reservoir cap was letting expanding intercooler coolant escape through the pressure hole. Remember, the intercooler cooling system is a closed system. No leaks were found in that system. Installer thinks the system was filled too high and is going to come up with a revised system for the reservoir. A smoke test was also performed and nothing was noted. We are still investigating what other issues there possible could be.
Obviously, I think we all expected to see a bigger/better result from the XB-1a. At the moment, they do not feel there is a boost leak. They think "maybe" this could be related to belt-slip with the 2.7 pulley and we are further investigating this. Belt tension is going to be checked and additional pulls with the 2.7 and 2.8 pulleys will be made with a full boost level recording (since the dyno boost gauge during the tuning pulls wasn't functioning consistently ) and see where we are at that point.