Larry Hampton
Member
- Joined
- September 28, 2009
- Messages
- 25
- Reaction score
- 0
- Location
- Central Oklahoma
- Year, Model & Trim Level
- '03 Sport Trac XLT 2wd
My daughter overheated her 2000 Explorer XLT 2wd back in July. Blew a intake gasket and cracked a head. Got a new head, valve job and surface on the other. Finally back together 6pm 12-31-11!! Bled the system with new 50/50, felt I had purged it good.
Drove it for 6 miles, CEL came on, ended up being the driver's O2 sensor never got plugged back in, but it never got hot. Sat till yesterday (when I finally figured out the unplugged wire) and tried to drive it into town, 4 miles the check gage light came on, temp was.pegged. pulled over, popped hood, cap puking. Hadn't been running heater, core has cold water, started and put defrost on high, temp went to 3/4, so I decided to limp back home, about 1/2 mile it went back to 1/2 and stayed there the whole way home. Got in Festiva and went on into town.
Got back, topped off coolant with more 50/50 (about 3/4 jug) and shut hood.
Got home tonight, checked fluid again, added a pint more, the overflow was full cold. Started it up, still no codes, warmed it for a couple minutes then drove about two miles with eye on temp gage, when all of a sudden the gage looks like a tach in a drag car. Pegged again. Turn around, defrost on high, back to driveway.
My thoughts are, maybe fan clutch went bad on her, or water pump.
Shaft seems okay, fan clutch 'feels' okay. Maybe my new Motorcraft T-stat is bad? I have the old one and a new gasket. No milkshake in new oil... Cooling system isn't pressurized by compression with cap off (I rented a cooling system test prior to putting the top end together).
I'm stumped.
Drove it for 6 miles, CEL came on, ended up being the driver's O2 sensor never got plugged back in, but it never got hot. Sat till yesterday (when I finally figured out the unplugged wire) and tried to drive it into town, 4 miles the check gage light came on, temp was.pegged. pulled over, popped hood, cap puking. Hadn't been running heater, core has cold water, started and put defrost on high, temp went to 3/4, so I decided to limp back home, about 1/2 mile it went back to 1/2 and stayed there the whole way home. Got in Festiva and went on into town.
Got back, topped off coolant with more 50/50 (about 3/4 jug) and shut hood.
Got home tonight, checked fluid again, added a pint more, the overflow was full cold. Started it up, still no codes, warmed it for a couple minutes then drove about two miles with eye on temp gage, when all of a sudden the gage looks like a tach in a drag car. Pegged again. Turn around, defrost on high, back to driveway.
My thoughts are, maybe fan clutch went bad on her, or water pump.
Shaft seems okay, fan clutch 'feels' okay. Maybe my new Motorcraft T-stat is bad? I have the old one and a new gasket. No milkshake in new oil... Cooling system isn't pressurized by compression with cap off (I rented a cooling system test prior to putting the top end together).
I'm stumped.