well...a new cap did not work. 2.5 hours later, truck was very hard to start. sooo....obviously the possibility is there that i need to reset the gasket, or i have another problem going on. But since the truck runs so well, i think i will just keep my system de-pressurized and deal with it for a while.
i did notice that with my modified cap, the coolant was back flowing into the tank. but i could hear it boiling.
i just cant help but think that something is going on with my cooling system. even before i replaced the gasket, there were several occasions that a large amount of coolant blew out past the radiator cap(after i filled the radiator full). its almost like the system built up too much pressure.
the truck runs cool, the gas mileage has increased(almost 16mpg with trailer and motorcycle running 80-90 mph) i have not had a chance to gauge it under normal driving, but this is a huge improvement. the power feels better than ever and i have no warning lights.
i am just going to deal with this for a while. the truck has 180k miles. if i can squeeze another 50k out of it, i will be satisfied.