jimster502
Well-Known Member
- Joined
- December 29, 2009
- Messages
- 196
- Reaction score
- 1
- City, State
- socal
- Year, Model & Trim Level
- 1997 Ford Explorer
Hey everybody,
So I just install a transgo shift kit (aka correction kit) and the car won't move in reverse. It seems as if it were to be in neutral. I've read other posts about the reverse not working but others don't have the same problem as mine. I took it out for a test drive and it seems to lag while I accelerate in D and hesitates to go into 2nd gear unless I manually shift it into 2nd. The car almost seems to feel as if if I were driving a manual transmission equiped car. Before I took it out for a test drive, there was smoking (from oil spill on cats) but as soon as I got back home (like 10 min after) I noticed it was still smoking and it smells like its the clutch burning(I put about 7 quarts of atf). The O/D light is flashing and I pulled a p1071 I believe. I read somewhere in the forums that the valve body needed to be torqued between 75-90 in/lbs. Correct me if I'm wrong. The valve body gaskets were replaced and the valve body was troqued to 80in/lbs. Anybody have any idea what I did wrong? The transmission was perfectly fine before. I was just trying to fix the transmissions factory issues( lag into reverse,clunk from 3rd-2nd gear,etc)
So I just install a transgo shift kit (aka correction kit) and the car won't move in reverse. It seems as if it were to be in neutral. I've read other posts about the reverse not working but others don't have the same problem as mine. I took it out for a test drive and it seems to lag while I accelerate in D and hesitates to go into 2nd gear unless I manually shift it into 2nd. The car almost seems to feel as if if I were driving a manual transmission equiped car. Before I took it out for a test drive, there was smoking (from oil spill on cats) but as soon as I got back home (like 10 min after) I noticed it was still smoking and it smells like its the clutch burning(I put about 7 quarts of atf). The O/D light is flashing and I pulled a p1071 I believe. I read somewhere in the forums that the valve body needed to be torqued between 75-90 in/lbs. Correct me if I'm wrong. The valve body gaskets were replaced and the valve body was troqued to 80in/lbs. Anybody have any idea what I did wrong? The transmission was perfectly fine before. I was just trying to fix the transmissions factory issues( lag into reverse,clunk from 3rd-2nd gear,etc)