bdkdave
Member
- Joined
- February 17, 2005
- Messages
- 17
- Reaction score
- 0
- Year, Model & Trim Level
- 2014 Explorer Sport
Hi Guys -
Thanks for all the GREAT information here. I'm going to ask for a little more, and hopefully help others at the same time.
The truck: My sister's 1996 Explorer 4.0L 2WD with 168k. Tranny was flushed and filled at 100k and never any issues until:
The "incident": My neice backed out into traffic, freaked, and dropped the truck into drive while still rolling backward. Truck lost 1st, but would move fine in manual 2 and then D once up to speed.
Took the truck to trusted repairman who had the problem pegged before we got there. Tranny was dropped, problem was as expected: overrunning / one-way clutch was broken, and a busted drum. Tranny was clean inside, no metal other than broken part. Part failed due to break rather than heating / burning. Parts replaced:
1) Torque Converter (at our request - better safe than sorry)
2) Drum
3) Overrunning / one-way clutch
4) Overhaul kit
5) Fluid and filter
Picked up truck and things seemed perfect. Started home (50 mile trip) and my sister pulled over a little before halfway back home. She said the truck just didn't feel right - it was revving too much. We switched cars, and I found the truck had lost overdrive. O/D light was flashing, and I limped it the rest of the way home....
(continued next post)
Thanks for all the GREAT information here. I'm going to ask for a little more, and hopefully help others at the same time.
The truck: My sister's 1996 Explorer 4.0L 2WD with 168k. Tranny was flushed and filled at 100k and never any issues until:
The "incident": My neice backed out into traffic, freaked, and dropped the truck into drive while still rolling backward. Truck lost 1st, but would move fine in manual 2 and then D once up to speed.
Took the truck to trusted repairman who had the problem pegged before we got there. Tranny was dropped, problem was as expected: overrunning / one-way clutch was broken, and a busted drum. Tranny was clean inside, no metal other than broken part. Part failed due to break rather than heating / burning. Parts replaced:
1) Torque Converter (at our request - better safe than sorry)
2) Drum
3) Overrunning / one-way clutch
4) Overhaul kit
5) Fluid and filter
Picked up truck and things seemed perfect. Started home (50 mile trip) and my sister pulled over a little before halfway back home. She said the truck just didn't feel right - it was revving too much. We switched cars, and I found the truck had lost overdrive. O/D light was flashing, and I limped it the rest of the way home....
(continued next post)