- Joined
- June 17, 2004
- Messages
- 24,502
- Reaction score
- 5,106
- City, State
- Knoxville, TN
- Year, Model & Trim Level
- 98 Limited AWD 302
I have replaced the wires, spark plugs, and ignition coil. And I did replace fuel injectors (including the one with the blown out o-ring).
Also the O2 sensor, even pulled the sensor out to rule out back pressure from a clogged cat.
The misfire is only partial, like an A/F mixture problem. Not even steady enough to set misfire codes.
I own lots of diagnostic equipment, even Factory stuff and I have access to Fords online stuff except for labor times.
This is just a weird problem probably caused by the nitrous backfire.
Maybe a cracked ring land but how do you test to prove that is the cause before tearing the engine apart?
Compression looks good 175-185 all cylinders, leakdown passes as they are all less than 20%.
My next test will probably be a running (dynamic) compression test.
Excellent work, I figured you had that all possible.
Given all the checks, the piston issue or similar wild things are viable thoughts. Mine would be wiring, given the age, brittleness, I'd think about checking continuity of items like the coil wiring, injector wires etc.