Well I am sure you've all been anxiously awaiting my account of the weekend!! Okay, so maybe not, but I like to think that you were... On to the large post:
My parts came on Friday and by 4:00 I had begun my repair work. In all of my planning though, I forgot one thing - to make sure that my digital camera had batteries... So no pics
On to the repairs... First off, I replaced the VMV. Replacing it through the panel in the floor was
very easy, and I recommend it to anyone who needs theirs replaced. Like I said, I started at 4:00. By 5:30, I had removed the driver's seat, pulled back the carpeting, removed the old VMV, and installed the new one. I did not have any trouble getting the pin lined up - I just used my left hand to guide the pin and held the VMV with my right hand. It was a bit of squeeze through the panel with both hands (I have the cuts on my hands and forearms to prove it), but I still think that this way would be easier than removing the cat. I do not think that it is possible to lose the pin inside of the tranny though... Granted, I could not see into it from the required angle to say for sure, but I did insert the pin and press and it would not go into the tranny. Also, it was sticking out of the VMV .2 inches, which I believe is the distance that Opera House said his was sticking out.
After the VMV, I dropped the transmission pan to replace the filter, check the valve body bolt torques, and replace the reverse servo O-rings. Now, I had never dropped the pan before (I always take it in for a complete fluid flush), but I was surprised by what I found: My tranny now has 120,450 miles on it without a rebuild, and there was not a trace of metal in the pan. Also, the fluid (which had 9,000 miles on it) looked basically brand new! It was red with a hint of black, which I am guessing came from the lubricating strip (Is that was this was?) stuck to the pan up near the front of it. I replaced the filter with the new one from bulkparts.com, and then checked the torque on the valve body bolts. They were a little less than what I wanted to set them at, but still within the acceptable range. By the time I had finished that, it was 7:00 and I was out of daylight.
7:00 AM Saturday I began again. First off, I replaced the reverse servo O-rings. I must say Opera House's directions were very good for this. I followed them, and the replacement went flawlessly. By 9:00, I had replaced the O-rings, put the pan and new gasket back on, and filled it up with 3.5 qts of fluid mixed with Trans-X. Then came the test: I started the truck and shifted into reverse. I didn't feel anything happen. But to my amazement, when I took my foot off of the brake, I began to move backwards!! Yes, the truck now shifts into reverse so smoothly that it
cannot be felt! I was so excited! No more clunking into reverse! The O-ring replacement was a great fix and I recommend it to anyone whose A4LD X clunks into reverse. So overall, the tranny work went well.
Then on to the engine work: Remove upper intake, clean it, replace gasket, retorque lower intake, and replace spark plugs and wires.
Removing the upper intake was fairly straightforward, and I did not run into any snags. I removed it, the IAC, and the throttle body. the IAC had been cleaned about 2 weeks earlier, so it was fine... The TB and upper intake were another story though! I cleaned all of the black crud off of the TB's butterfly valve and also cleaned out the springs on it and oiled them. Works great now. For the upper intake, I think that it is impossible to get the inside of it shiny, but I did get it to the point where no black crud would come off of it when I rubbed my finger on any inner surface of it. In total, I used about 42 oz of Gumout!

So now the upper intake is free of 120,000 miles worth of buildup. I'm sure it is much better now. With the upper intake off and a lot of stuff disconnected, I started on the plugs. Driver's side was easy, so were the first two plugs on the passenger side. By easy I mean that I could get to them all from on top of the truck. The 3rd plug on the passenger side took a little more work, but with 2 extensions, a universal socket, and a spark plug socket, I was able to get it out and replace it by accessing it through the wheel well. No, I do not have a lift... The truck was not jacked up and the wheel was still on as well. So it can be done. I then checked the torque on the lower intake manifold bolts. They were loose. I tightened them up in stages to 216 in-lbs. With spark plugs and wires replaced, I gave the upper intake and throttle body one last check and dried them out thoroughly, then put everything back together and started the truck. It was 5:30 on Saturday, and I had finished.
WHAT A DIFFERENCE!!!
I no longer have a rough idle or odd A/F ratio gauge behavior. Throttle response is better and my hesitation/lack of power problems are gone. The tranny shifts smoothly and reverse is clunk-free. Here's the best part (in my opinion): I used the adjustable VMV from bulkparts.com, which allows you to modify when the tranny shifts gears while in drive. Well, I adjusted it a bit to take full advantage of my SuperChip and all I can say is "Wow". The truck really moves now! I set it to shift higher than stock and now the engine will rev to about 4,500 RPM before shifting (when I floor it - normal driving is pretty much the same) Naturally, I had to make sure that it would shift through all of the gears so I got on the highway and hit top speed (105 mph) faster than I ever have! I love it! The adjustable VMV is definitely the way to go if you've ever wished your auto tranny would shift at a higher RPM.
Just to recap, to fix all of my problems I did the following:
- Replaced the fuel filter
- Changed spark plugs and wires
- Replaced Reverse Servo O-Rings, main O-ring with updated "double-lip" style from bulkparts.com
- Replaced Vacuum Modulator Valve with adjustable type from bulkparts.com
- Replaced transmission filter with improved version from bulkparts.com
- Checked and retorqued Transmission Valve Body bolts
- Removed and cleaned upper intake and throttle body
- Replaced plenum gakset
- Retorqued lower intake manifold bolts