rp23g7
Member
- Joined
- November 1, 2006
- Messages
- 47
- Reaction score
- 0
- City, State
- washington
- Year, Model & Trim Level
- 99 ford explorer
So, i finished my 0012M fix yesterday, well most of it.
I replaced the upper and lower O rings, kinda puzzled at Ford, dont see any reason they actually make the intake manifold in two pieces.
Both sets were rock hard, and you could see on the lower where it was leaking through the seal. Sorry, i didnt take any pictures.
I didnt replace the tensioner, as the part looked completley different, and i didnt want to take something apart and find that the part wouldnt work.
The factory one has a hex head on it, the replacement in the kit had the hex and then the machining extended another inch or so above, it looked like it wouldnt clear the temp sensor, i did however put the restrictor and the new plug in, that seemed to really help a lot.
Put everything back together and it idled like crud, looked for something i forgot, turned out i didnt reattach the PCV hose to the back of the manifold.
Took it for a drive and it ran and idled really good, had to wait till morning to see if the fix worked though.
Started it up this moring and it started and idled by itself. I dont ever remember it not doing the high rev at startup, and we bough it new.
I replaced the upper and lower O rings, kinda puzzled at Ford, dont see any reason they actually make the intake manifold in two pieces.
Both sets were rock hard, and you could see on the lower where it was leaking through the seal. Sorry, i didnt take any pictures.
I didnt replace the tensioner, as the part looked completley different, and i didnt want to take something apart and find that the part wouldnt work.
The factory one has a hex head on it, the replacement in the kit had the hex and then the machining extended another inch or so above, it looked like it wouldnt clear the temp sensor, i did however put the restrictor and the new plug in, that seemed to really help a lot.
Put everything back together and it idled like crud, looked for something i forgot, turned out i didnt reattach the PCV hose to the back of the manifold.
Took it for a drive and it ran and idled really good, had to wait till morning to see if the fix worked though.
Started it up this moring and it started and idled by itself. I dont ever remember it not doing the high rev at startup, and we bough it new.