Been a long time since I've been in here and now I'm stuck at home bored and not working, so thought I'd update. I spent 4 days in Death Valley in January which turned out to be one of the most incredible trips. It was a group of 12 of us from all over the world including CA, NY, Denmark, Sweden, and London. Most of us didn't know each other at the beginning, and most people had never done anything like this or had even been offroad before. We were in 5 vehicles, including the Mountaineer, a Cherokee, stock TRD Tacoma, a VW Touraeg, and a rental Jeep Rubicon. We went all over the national park, covered over 300 miles offroad and about 1400 in total. There are probably hundreds of photos taken from the trip but here are a few.
On the second day I noticed one of my AC hoses was rubbing on the AC compressor pulley so I had to ratchet strap the hose out of the way, and run the rest of the trip without AC. Then on the 500ish mile drive home the AC compressor pulley gave up the ghost and left me and 2 Swedes stranded at a gas station in the middle of nowhere on interstate 5 at 1am. The 2 others had a flight back to Sweden the next day, and luckily the Cherokee was about an hour behind us, so when he arrived we swapped some of his luggage for the 2 Swedes and they continued the 140 miles home and I waited another 9 hours for a tow truck to come. Thankfully things worked out the way they did, everyone made it to their destinations, I was within my AAA towing range and this didn't happen on the side of the highway or in the middle of Death Valley a hundred miles away from civilization.
I now have a shorter belt that I will keep with me as a spare, and I just finally got around to replacing the compressor and the hoses. At the same time I decided to take another stab at improving the steering. The power steering pump was whining a little, and the autozone steering box I had was super loose, and when I did the TTB conversion I had initially tried hydro assist but messed up when drilling and tapping the box, so I gave up on it at the time, so I wanted to try again. I got a rebuilt and ported box from Minh Worx and tried it again, only to realize that the stock steering pump isn't powerful enough to push the ram. With the ram assist on it felt like the tires were stuck up against a wall, making it sometimes impossible to turn the wheel at all. So for a second time I've had to give up on hydro assist. Maybe down the road I will try to figure out how to adapt another pump to my motor. The available Saginaw pump conversions necessitate eliminating the AC which I don't want to do.
So now the next hurdle is what to do with my motor. When I had the head gaskets done my mechanic friend accidentally cracked my oil pan, and the JB weld repair is currently leaking. So I'm weighing my options on what to do next, whether I can fix it with the oil pan installed, pull the motor so that I can remove the oil pan and fix it correctly, rebuild the tired old motor while it's out, or get a different motor. Buying a refurbished long block scares me because of all of the horror stories about issues and warranties not being honored.