I have to ask is it worth every dollar spent?
Cause it sure looks bad@$$!![]()
Well boys, here we go again!
At least it isnt too late for me to learn from JD's rather painful experience and take steps against this happening to me in my build.
Stupid stretch (tty) head bolts. Another bad idea when you start making a motor do stuff it was never designed to do.
so, over 10.5 compression and 10lbs boost is bad. I was at about 9.5:1 compressions with 10 lbs boost. I wonder what JD's heads will be like. Id be interested to find out if they are warped and cracked also.
I think were pretty safe to say that JD will have the strongest 4.0 ohv of anyone on this board, ever!
It is strange that compression is still really good. That one blug looks like it wasnt firing anymore at all.
I do want to see what the head gasket looks like. Your not going to pull the motor to get the heads off are yo?
definatly do the leakdown test, may only have to pull one head for now, or may find its an intake issue
not really seeing any signs of burning coolant on the plugs, those look like burning just a tad rich. burning coolant usually turns the plugs white and leaves deposits, and if its really bad you will find the plugs really clean, looking almost new
You could have a crack in the head in the intake runner pulling water in only when running hence the good compression numbers.