Got the brakes bled, thanks to the help of a friend, and took the rig for another small test ride. Seems good for today.
So afterwards, we found the brake lights was stuck on, and when wiggling the pedal they flash at the same time it is manhandled. We also discovered my neon 3rd brake light no longer works. It worked perfectly, before I sent it to the shop. Just had it inspected and new tags right before it was sent off to them. Ok... wtf?
Wait a second....Let's back up a bit here. I need to get this thread fixed, and back on track.
A little back ground first, to put things into perspective. This post is for the sake of this thread, and the rigs history. People have been wanting to know what the hell has been going on these past months. This is the only post made about any of this, and anywhere to date. I was trying to avoid doing this, but it seems I have come up against some issues, that I will need the forums help with. Here it is in the open, and once this is said, I do not want to continue it any further. It is part of this rigs history, and everything to date has been documented this far. I felt this thread would not work correctly, with this info missing. Like ripping out a few chapters in a book. I will provide some details, and the ones that will matter for future work & posts only. It's long, and bad enough as it is. If you don't want to read about stupid drama, I don't blame you, just change the channel.
So....What was done?
The rig is now OBDII with a 98 5.0L, and fully rebuilt auto trans. Atlas had the spline shaft and adapter ring swapped. Trans output shaft was shortened by 3/4" for the Atlas. I didn't want to deal or even try to deal with the electrical headaches that this job required. I can swap engines & transmissions in my sleep, and the occasional wiring work, but this EEC swap, was more then I wanted to handle. I knew of a small home shop elsewhere, that said they are the best in the bizz at this work. I contacted them, told them all that I wanted done, and asked for a price. We came upon an agreement for parts, labor, & a time frame. A few months later, and I gave them the rig, money, and a bunch of brand new parts. I have talked and met them in the past, and they seemed trust worthy enough. If you know me, that is saying something.
Facts, not *****ing, just the facts...
Communications from here on out was nothing short of terrible. Questions asked was ignored, or half answers, and vague at that. Parts sent for install was no not being done, for one reason or another. I gave them 3/4 of the agreed upon price and a few days before it was scheduled to be picked up, I asked for the total balance owed. They gave it, and I paid it that day. I wanted to make sure they had it before the trailer arrived for pickup. All good. During that call, I was told they have a few things to do still, but will be done with days left to road test everything for any bugs to fix. Cool, sounds good so far.
So 14 weeks later, and the (extended) deadline for the pickup had come. A few hours before the driver showed, I called and asked if all was good, if a test ride was performed, and anything I need to know about. I was told everything was done, and no issues, and ready to load and go. Cool. Driver showed late that day, but he showed. He called me, and said it's loaded, but there was something wrong with the truck. When he asked them, they told him, they informed me of the issue already, and all was good, so he left. Hmm...
So that issue was the fuel gauge wasn't working, and they had sent me a FB message, after the delivery driver loaded up and left, that there was an issue. Later that night, when I seen it, I responded and asked about the mystery issue. I was informed the wire broke on the sender the day it was loaded to leave, and nothing they could do about it. ( see a few posts back as to why it broke) Ok, hmm...
Truck makes it back home.
When we took it off the trailer, it was puking coolant. The front right wheel locked up all the way off onto the road. Then the brake pedal went to the floor. It was in 4low to get on/off the trailer, but wouldn't go back into 2H. After fighting the shifter for an hour, we got it back into 2Low, and into the driveway. It was then we noticed the brake lights was stuck on, but the delivery guy didn't mention the 3rd light at that time.
So I sent a message to the shop that had it for 14 weeks, and let them know what had just happened. They said the brake switch was bad, would send a new one, along with parts to fix the fuel gauge. I found the coolant leak was from the new upper hose not fastened. Easy fix, no biggie. They did offer to pay to have a shop do the fuel repair, but I declined, as I knew how to do it. That was as far as the niceties went. All downhill from here.
As the initial inspection resumed, I slowly found a bunch of things wrong, missing, or non existent. (I will post these as I fix them, one at a time.) I have never seen a job done by anybody claiming to be the best in the bizz, look so amateurish. It was blatantly obvious, they ran out of time, and didn't finish. If I knew they needed a longer extension ahead of time, I could have asked my driver if he could handle it or not. After 14 weeks, I wouldn't have minded another week.
I tried to contact them by phone to just talk about this stuff, no luck. They prefer doing bizz by FB messenger over actually speaking on the phone, and I had to send a message. The response was rude & ignorant as far as I am concerned. Being told I do not give credit & praise, for the good work done, and only complain about the bad stuff, made me a bad guy. Well, hang on a minute, I have to have a chance to test the rig first, don't I? Can't do that, when it was returned inoperable.
The agreed up on time frame was even extended by 2 weeks, as the delivery driver managed to manipulate his schedule with his normal day job. He was a trusted friend, that took the side job for this. I then asked for my parts they forgot/neglected to send me with the rig. I asked what the warranties are, and how to handle that, if needed. They ignored me. I never got an answer, or the parts. Hmm... I checked FB again, and read another name calling hateful message. I responded by telling them, calling me names, will not end well for them. The response was them playing dumb. I wasn't going to argue and be as immature, and give response again.
Eventually a package arrived with a Chinese knock off sending unit, and a used brake switch. I installed both. A short trip around the block, revealed the brakes was still soft, and needed more attention. Upon this down time, more issues and stupid **** was found. At this point, all I can do is shake my head, and figure out, how I will ever be able to trust this rig again? So there it is, you pretty much up to speed now. Time to move forward, and get this rig fixed, and trip ready.
Back to today's work, and these damn bloody brakes.
Nothing works for bleeding this thing, except a good old foot pump bleed. I don't know why, it is, what it is. Rig has sat ever since, until today, when I finally got someone to help bleed them.
So now, I can see the used brake switch they sent as a replacement not working right, but the 3rd brake light? Something is up, as I don't see how the Neon ballast can go bad just sitting since last October. The only thing I know what to do with that, is to disconnect the gray round tow harness connector, and clean it real good. Other than that, I'm stumped. Battery is disconnected now. I will get a new pedal switch, and if the same thing happens again, I know it is the wiring going to the switch. Hmm.... Great.
So while the bleed was done, we found the dr side 02 was loose, and the wires up against the exhaust. Fixed that and added some zipties to the wires.
We found the A/C accumulator mount was not on, and the bolt bracket laying on top of the exhaust manifold. Need to find the right bolt for that still.
While looking around that area, we discovered that the relay box for the CAD function was hanging by a single 16ga wire, and made it's way towards the fan shroud. It is just flopping loose. I have to remove the filter duct work to be able to get in there and mount it back to the core, where it will stay put. I couldn't imagine what could have happened if I didn't see this, and it got chewed up by the fan, and thrown into 4wd with a locker at hwy speeds. Scary **** to think about. Just glad we seen it, when we did.
Upon the test ride, the new drive train was finally put under the pressure of the skinny pedal, and gone thru the 1st-3rd. It has a slight stumble upon launch, but recovers. There is absolutely no feeling of the TransGo shift kit (supposedly) installed in the rebuilt Auto trans. If this is what it feels like with one, I hate to feel it without one. Sheesh, it must be a lazy shifting slug. A manual is instantly responsive to the skinny pedal. Such a difference to get used to in this rig.
Been raining for a couple days, and at least 5 days in a row in the forecast, so when I do get time from work, & nature allows, I will get more done, and share previous work, and upcoming work. There is a lot to share, and document.
It has been a heck of a stressful few months for me with this rig, and I can't wait to get it back on the trails. Wheeling season is already here, and I am late to the dance!